首页|期刊导航|铁道标准设计|基于应力流理论的垂、横向刚度解耦型浮轨扣件理论设计方案研究

基于应力流理论的垂、横向刚度解耦型浮轨扣件理论设计方案研究OA

Research on Theoretical Design Scheme of Vertical and Lateral Stiffness-Decoupled Floating Rail Fasteners Based on Stress Flow Theory

中文摘要英文摘要

传统浮轨扣件以较低垂向刚度实现较高减振效果而得到大规模应用,但因其横向刚度较低,导致钢轨横向动态位移较大.为提升浮轨扣件抵抗横向荷载能力,根据实际尺寸建立浮轨扣件精细化有限元模型,以应力流理论为根本、传力路径为基础对扣件结构进行优化设计,通过室内实验测得改进后扣件垂向、横向荷载-位移曲线,在与实验结果对比基础上获得改进前后浮轨扣件刚度变化情况,并研究改进前后浮轨扣件在正常服役状态下各部分应力应变情况,实现扣件刚度解耦设计.结果表明:浮轨扣件在垂向荷载、横向荷载作用下荷载-位移曲线表现出明显非线性特征,钢棒以垂直垂向主应力、平行横向主应力的方式填入橡胶楔块改变力流在扣件结构中的流动路径,路径变短、线形变直、扣件结构刚度增加,改进后新型浮轨扣件垂向刚度增加 1.05 kN/mm,约 15.5%,横向刚度增加 4.81 kN/mm,约 56%;加入钢棒后扣件系统发生塑性变形的预压力限值从 1.688 MPa下降到 1.41 MPa,但在正常服役状态(预压力 0.8 MPa)下,扣件系统仍可以保持良好工作性能,硫化质量棒与橡胶楔块接触区域变形连续未出现撕裂,橡胶楔块最大形变量从 1.17 mm减少到 0.89 mm,约 20%.

The traditional floating rail fastener is widely used due to its low vertical stiffness,which can achieve a high vibration damping effect.However,its low lateral stiffness results in a large transverse dynamic displacement.In order to improve the transverse load resistance of the floating rail fastener,a refined finite element model of the fastener was established based on its actual dimensions,and the fastener structure was optimized using stress flow theory as the fundamental principle and the load transfer path as the design basis.The vertical and lateral load-displacement curves of the improved fastener were determined via laboratory experiments.By comparing these experimental results before and after improvement,the stiffness variations of the floating rail fastener were quantified.The stress and strain distributions of each component of the floating rail fasteners before and after improvement under normal operating conditions were examined,thereby achieving a stiffness-decoupled design of the fastener.The results showed that the load-displacement curve of the floating rail fastener exhibited pronounced nonlinear characteristics under both vertical and transverse loads.The rubber wedges were designed to be filled with steel rods oriented perpendicular to the vertical principal stress and parallel to the transverse principal stress,thereby altering the stress flow path within the fastener structure.This adjustment shortened the pathway,straightened its trajectory,and consequently increased the overall stiffness of the fastener structure.After the improvement,the vertical stiffness of the new floating rail fastener increased by 1.05 kN/mm,about 15.5%,and the lateral stiffness increased by 4.81 kN/mm,about 56%.After the addition of steel rods,the pre-pressure limit of plastic deformation of the fastener system decreased from 1.688 MPa to 1.41 MPa,but the fastener system maintained stable operating performance under normal service conditions,with a pre-pressure of 0.8 MPa,and the contact area between the vulcanized test rod and the rubber wedge exhibited continuous deformation without tearing.The maximum deformation of the rubber wedge decreased from 1.17 mm to 0.89 mm,a reduction of approximately 20%.

汪虎;赵才友;雷佳鑫;陈江雪

西南交通大学高速铁路线路工程教育部重点实验室,成都 610031||西南交通大学土木工程学院,成都 610031西南交通大学高速铁路线路工程教育部重点实验室,成都 610031||西南交通大学土木工程学院,成都 610031西南交通大学高速铁路线路工程教育部重点实验室,成都 610031||西南交通大学土木工程学院,成都 610031中国铁路设计集团有限公司城市轨道交通数字化建设与测评技术国家工程研究中心,天津 300308

交通工程

浮轨扣件应力流室内实验有限元仿真扣件刚度结构改进

floating rail fastenerstress flowlaboratory experimentfinite element simulationfastener stiffnessstructural improvement

《铁道标准设计》 2026 (2)

46-53,75,9

国家自然科学基金项目(KYL2023JZ01)国家重点研发计划自主项目(2022YFB2603404)

10.13238/j.issn.1004-2954.202404170003

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